Poor Process Safety Mgt Led to Fatal Chem Plant Blast

Friday, October 28, 2016 @ 05:10 PM gHale


Workers flee the explosion and fire at Williams Olefins Plant in June, 2013.

Workers flee the explosion and fire at Williams Olefins Plant in June, 2013.

Two employees died and 167 injured because of process safety management program deficiencies at the Williams Olefins Plant in Geismar, Louisiana, over 12 years that allowed a “reboiler” to remain unprotected from overpressure, and ultimately rupture, causing an explosion on June 13, 2013.

The Williams Geismar facility produces ethylene and propylene for the petrochemical industry and employs approximately 110 people. At the time of the incident, 800 contractors worked at the plant on an expansion project aimed at increasing the production of ethylene.

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The incident occurred during non-routine operational activities that introduced heat to a type of heat exchanger called the reboiler, which was offline and isolated from its pressure relief device. The heat increased the temperature of a liquid propane mixture confined within the reboiler, resulting in a dramatic pressure rise within the vessel. The reboiler shell catastrophically ruptured, causing a boiling liquid expanding vapor explosion (BLEVE) and fire, which killed two workers; 167 others reported injuries, the majority of which were contractors.

The Chemical Safety Board (CSB) investigation revealed a poor process safety culture at the Williams Geismar facility, resulting in a number of process safety management program weaknesses.

These weaknesses include deficiencies in implementing Management of Change (MOC), Pre-Startup Safety Review (PSSR), Process Hazard Analysis (PHA) programs, and procedure programs causal to the incident:
• Failure to appropriately manage or effectively review two significant changes that introduced new hazards involving the reboiler that ruptured — (1) the installation of block valves that could isolate the reboiler from its protective pressure relief device and (2) the administrative controls Williams relied on to control the position (open or closed) of these block valves.
• Failure to effectively complete a key hazard analysis recommendation intended to protect the reboiler that ultimately ruptured.
• Failure to perform a hazard analysis and develop a procedure for the operations activities conducted on the day of the incident that could have addressed overpressure protection.

“The tragic accident at Williams was preventable and therefore unacceptable,” said CSB Chairperson Vanessa Allen Sutherland. “This report provides important safety lessons that we urge other companies to review and incorporate within their own facilities.”

The CSB case study shows:
• Using a risk-reduction strategy known as the “hierarchy of controls” to effectively evaluate and select safeguards to control process hazards. This strategy could have resulted in Williams choosing to install a pressure relief valve on the reboiler that ultimately ruptured instead of relying on a locked open block valve to provide an open path to pressure relief, which is less reliable due to the possibility of human implementation errors
• Establishing a strong organizational process safety culture. A weak process safety culture contributed to the performance and approval of a delayed MOC that did not identify a major overpressure hazard and an incomplete PSSR
• Developing robust process safety management programs, which could have helped to ensure PHA action items were implemented effectively
• Ensuring continual vigilance in implementing process safety management programs to prevent major process safety incidents

Following the incident, Williams implemented improvements in managing process safety at the Geismar facility.

Improvements in Place
These improvements include redesigning the reboilers to prevent isolation from their pressure relief valves, improving its management of change process to be more collaborative, and updating its process hazard analysis procedure.

“Williams made positive safety management changes at the Geismar facility following the accident, but more should be done to improve process safety and strengthen the plant’s process safety culture,” said Investigator Lauren Grim. “Our report details important safety recommendations to protect workers at the Williams Geismar facility.”

To prevent future incidents and further improve process safety at the Geismar plant, the CSB recommended Williams strengthen existing safety management systems and adopt additional safety programs. These strategies include conducting safety culture assessments, developing a robust safety indicators tracking program, and conducting detailed process safety program assessments.

The CSB also identified gaps in a key industry standard by the American Petroleum Institute (API) and issued recommendations to API to strengthen its “Pressure-relieving and Depressuring Systems” requirements to help prevent future similar incidents industry-wide.

“Most of the accidents the CSB investigates could have been prevented had process safety culture been a top priority at the facility where the incident occurred,” Sutherland said. “These changes must be encouraged from the top with managers implementing effective process safety management programs.”

Click here to review the entire final report.



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